Hi..
i just finished soldering and setting up for a bench test... i am using the wiki as a guide.
I want to use PWM Input.
I think i connected everything as it should be.
LED1 is blinking, i updated the firmware and it said ok and on reboot it says:
[05:15:54.86] Reboot command received...
[05:15:56.36] Gluonpilot v0.5.2 [Jan 28 2011 11:27:31, config: 266B, logline: 56B, navigation: 504B, double: 4B]
[05:15:56.37]
[05:15:56.37] A RESET instruction has been executed
[05:15:56.38] Found hardware version v0.1n
[05:15:56.38] 1 MB flash found
[05:15:56.38] Loading configuration...done
[05:15:56.46] Waiting for pwm..done
[05:15:56.48] Control task initializing...done
[05:15:56.78] Sensors task initializing...done
[05:15:56.79] Gps & Navigation task initializing...
[05:15:56.79] Console input task initializing...done
[05:15:56.80] Datalogger task initializing...done
[05:15:56.80] Telemetry task initializing...done
[05:15:56.81] OSD task initializing...
[05:15:56.82] no OSD found!
[05:15:57.29]
[05:15:57.29] !
[05:16:02.33] Gps & Navigation task initialized
But when i wiggle the controls on my RC-transmitter... nothing happens in the RC-Input tab.
I am using a Futaba T12FG with 40Mhz and a Corona RP8D1 receiver. When i unplug a channel and plug in a servo, the servo is working properly.
Any ideas? I tried with 2,4Ghz and a Futaba R617FS Receiver before... same problem..